sling Posted November 24, 2008 Report Posted November 24, 2008 Check this one here http://tvtotal.prosieben.de/components/vid...band.html?mode= Quote
Elvis Posted November 24, 2008 Report Posted November 24, 2008 Skids is right...this one has been around for a while and has been posted here before. If memory serves the pilot was killed in a crash. BO 105...fully rigid system...don't try this in your Jetbox. Mark NTSB Identification: NYC89FA220 . The docket is stored on NTSB microfiche number 43340. Accident occurred Wednesday, September 20, 1989 in TUCKERTON, NJ Probable Cause Approval Date: 9/9/1992 Aircraft: MBB BO-105CB-4, registration: N5353V Injuries: 1 Fatal. THE HELICOPTER ENTERED A SHALLOW CLIMB & STEEP TURN AT LOW ALTITUDE. ALTHOUGH THE PILOT INITIATED A RECOVERY, THE HELICOPTER STRUCK THE GROUND BEFORE HE RECOVERED. AN INVESTIGATION REVEALED NO PRE-EXISTING FAILURE OR MALFUNCTION WITH THE ENGINE OR AIRFRAME. A PERFORMANCE STUDY SHOWED THE MANEUVER HAD A MAXIMUM BANK OF 98 DEGREES & A MAXIMUM ALTITUDE OF 75 FEET AGL. RECOVERY WAS NOT INITIATED UNTIL .5 SECONDS AFTER THE APEX OF THE MANEUVER. The National Transportation Safety Board determines the probable cause(s) of this accident as follows: THE PILOT'S DELAY IN REMEDIAL ACTION BY DELAYING THE PULL-UP FROM A DESCENDING MANEUVER. Quote
sling Posted November 24, 2008 Report Posted November 24, 2008 NTSB Identification: NYC89FA220 . The docket is stored on NTSB microfiche number 43340. Accident occurred Wednesday, September 20, 1989 in TUCKERTON, NJ Probable Cause Approval Date: 9/9/1992 Aircraft: MBB BO-105CB-4, registration: N5353V Injuries: 1 Fatal. THE HELICOPTER ENTERED A SHALLOW CLIMB & STEEP TURN AT LOW ALTITUDE. ALTHOUGH THE PILOT INITIATED A RECOVERY, THE HELICOPTER STRUCK THE GROUND BEFORE HE RECOVERED. AN INVESTIGATION REVEALED NO PRE-EXISTING FAILURE OR MALFUNCTION WITH THE ENGINE OR AIRFRAME. A PERFORMANCE STUDY SHOWED THE MANEUVER HAD A MAXIMUM BANK OF 98 DEGREES & A MAXIMUM ALTITUDE OF 75 FEET AGL. RECOVERY WAS NOT INITIATED UNTIL .5 SECONDS AFTER THE APEX OF THE MANEUVER. The National Transportation Safety Board determines the probable cause(s) of this accident as follows: THE PILOT'S DELAY IN REMEDIAL ACTION BY DELAYING THE PULL-UP FROM A DESCENDING MANEUVER. The accident occured while making a movie as i understand....i've been tryng to get the tape on Google but no sucsses. Also,(a bit out of topic sorry!) there is the existence of a documentary made by TC about LTE, if somebody know what i'm talking about, please PM me. Quote
Gary Watson Posted November 24, 2008 Report Posted November 24, 2008 You're right about this being around for a while as I saw it at Dome Pete courstesy of the MBB guys when we purchasea Bow Kow in the early 80s. AFAIK it was used as a marketing tool showing the rigid rotor performance. I've been to around 100 Deg bank in the back of our Bow Kow (thanks to DT) over the drill ships in McKinley bay in the Beaufort. This was with a 105 that was tarted up with every piece of gear known to mankind. Quote
chopper doctor Posted November 26, 2008 Report Posted November 26, 2008 Yes, do not try this at home kids. http://www.break.com/usercontent/2006/7/Bo...ics-135033.html Quote
skullcap Posted November 26, 2008 Report Posted November 26, 2008 this is 2nd time in a matter of days this video is posted, not sure why, is there anything to learn from watching this fatal accident???? This pilot was a very experienced aerobatic pilot who had done the same manuever many times,,,,,pointless kind of like posting an abortion on a mom and tots forum I think,,,,jmho Quote
Wiggins Posted November 27, 2008 Author Report Posted November 27, 2008 this is 2nd time in a matter of days this video is posted, not sure why, is there anything to learn from watching this fatal accident???? This pilot was a very experienced aerobatic pilot who had done the same manuever many times,,,,,pointless kind of like posting an abortion on a mom and tots forum I think,,,,jmho I gotta say I agree with you on this one. I prefer happy ending! Quote
R22Captain Posted December 5, 2008 Report Posted December 5, 2008 Looks like a typical 0.2 between camp and 11-25 booster, hey r22captain?? hahhaha how right you are. BOOSTER DOWN!! Quote
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